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    new downpipe, test pipe and filter... still only sees 5-6psi...

    clutch is solid. OEM with less than 5k miles. Im pretty sire the problem isnt in the exhaust. Ive been searching here for the last few days and found some interesting things. Ive also driven the car for the last day or two and have noticed some other minor issues, so Im going to be...
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    Indiana ST185 nut - MK3 owner wanna be

    You know, I didnt like them in pictures either until I saw them in person and then picked them up. theyre 3 piece custom made 18 inchers. wide and light. Anywho, Glad you finally got on here bro. After owning an ST165 I can vouch for the complete and total pain in the royal ass that is...
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    2007 INDIANA MEET DISCUSSIONS

    count me in too if this thing happens.
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    new downpipe, test pipe and filter... still only sees 5-6psi...

    for the sake of learning, whats the reasoning behind that suggestion?
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    new downpipe, test pipe and filter... still only sees 5-6psi...

    still. looks like they did a decent job with them.
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    new downpipe, test pipe and filter... still only sees 5-6psi...

    Look pretty similar. are those 3 piece? here they are up close Works VS-SS ok, were now WAY off topic. sorry.
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    new downpipe, test pipe and filter... still only sees 5-6psi...

    so did you have that custom made or did you use the magnaflow with a cooleeze kit or something like that? That looks slick.
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    new downpipe, test pipe and filter... still only sees 5-6psi...

    Yeah, I own a security company and I need the room and economy to haul a bunch of cable and security cameras around. Dirt slow, plenty of room and 35mpg makes me happy for a daily. The slow, funky gas mizer helps fund the Supra habit. I learned years ago the problems with modifying my daily...
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    new downpipe, test pipe and filter... still only sees 5-6psi...

    WHAT IS THAT?!?!?!?! Ive been thinking about making a 3" with a dual tip straight through muffler, but theyre hard to come by. If someone already makes one Im all over that. oh boostlee, Ive seen your car around Greenwood, but Im usually driving my Xb so theres no point in waving. Oh, the...
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    new downpipe, test pipe and filter... still only sees 5-6psi...

    Well, I drove the piss out of it today and also checked all the boost hoses, no issues that I can find. Ill be replacing all the vacuum hoses this week and Im gonna try to find a 3" cat back I can pick up try to aleve the one bottleneck in the system and fix that one exhaust leak (even though...
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    new downpipe, test pipe and filter... still only sees 5-6psi...

    As for shimming the wastegate I dont want to go upping the boost artificially just yet. I want to be sure the car is running as strong as possible efore going that route simply because the maintenance history is a little questionable (read: idiot PO) MKIIIMan089, the roblem is that even running...
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    new downpipe, test pipe and filter... still only sees 5-6psi...

    Ok, Every turbo car I have ever owned I have seen increases in efficiency by removing cats, installing higher flowing downpipes, and higher flowing air filters etc... The Supra doesnt appear to respond the same way.. heres the story- 89 Supra Turbo. Picked it up with a blown headgasket. Put...
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    did the hg, now codes and idling problems.

    Sent you a PM Matt. Anyways, thanks to all for confirming my suspicions. Mainly wanted to introduce myself and the car outside of the midwest forum. Thanks for the help. Armando
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    did the hg, now codes and idling problems.

    OH! and Matt... Do you have an extra EGR tube I can modify to make a block off plate?
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    did the hg, now codes and idling problems.

    That sounds good. let me know if youre heading up here. Ill be busy after 7 or 8 though. and yeah the stockers are in great shape.
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    did the hg, now codes and idling problems.

    Tested the TPS today, results = either the TPS is not functioning or Im measuring the clearance at the wrong screw. LOL. I reset the codes, Ill check it her ein a little while when I gof ro a drive and see if it still throws the same codes. In the meantime Im gonna call Todd on Monday and...
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    did the hg, now codes and idling problems.

    Its a US head. Car came with a Jap engine so I dont have an old EGR to do that to. :( intake mani is Jap so I cant really run emissions back on it. I made a temp plate, but trust me... it wont work for very long. And I KNOW its leaking some. The second head I had that I swapped in when I did...
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    did the hg, now codes and idling problems.

    one more issue... theres an EGR port on the intake side of the head by the intake mani. anyone know a good place too get a block off plate? aside from just taking my template to a machine shop.