ok, i just got back from NOPI @ budds creek,and last nite i made 2 runs
1st run: Red lighted -.074
60 foot- 2.943
330- 8.003
1/8 - 12.136 @60.41 mph
1000 foot - 15.589
1/4 - 18.526@76.70mph
second run is not even worth typin as you will see in a few...
MODS: BIC DDP,test pipe,2 3/4" exhaust from there with no muffler,stock boost,and auto tranny...fresh mani gasket...
now for the story: now remember i have never been in a MK3 befor so i do not know how it is supposed to feel power wise... any way, i ran the 1st run as i posted and really didnt have much power , my second run i get to the line take off with a .52 reaction time and as soon as i hit 2nd gear all power was gone....i let off the pedal for a second ,then floored it again ..there was still no power... i parked the car until this morning got up and went on my way back to nopi it ran kinda ok for the 1st mile then it did basically the same thing it did the night befor .everytime i try to get into boost it kinda boggs down and a little black smoke comes out until i let off the pedal or get out of boost. i have another MK# owner drive the car while i was at the track to see if he could gimme a idea on what it could be.he drove it about 100 yards and said that it was probably an leak in the innercooler pipe somewhere...my thing is if it was a leak would it still hold the boost at 6psi?? ...it is about a half pound lees than what it usually boosts at..all i know is it should have ran alot faster than 18 seconds in the quater,and it has never ran as bad as it is now!! any input is appreciated
1st run: Red lighted -.074
60 foot- 2.943
330- 8.003
1/8 - 12.136 @60.41 mph
1000 foot - 15.589
1/4 - 18.526@76.70mph
second run is not even worth typin as you will see in a few...
MODS: BIC DDP,test pipe,2 3/4" exhaust from there with no muffler,stock boost,and auto tranny...fresh mani gasket...
now for the story: now remember i have never been in a MK3 befor so i do not know how it is supposed to feel power wise... any way, i ran the 1st run as i posted and really didnt have much power , my second run i get to the line take off with a .52 reaction time and as soon as i hit 2nd gear all power was gone....i let off the pedal for a second ,then floored it again ..there was still no power... i parked the car until this morning got up and went on my way back to nopi it ran kinda ok for the 1st mile then it did basically the same thing it did the night befor .everytime i try to get into boost it kinda boggs down and a little black smoke comes out until i let off the pedal or get out of boost. i have another MK# owner drive the car while i was at the track to see if he could gimme a idea on what it could be.he drove it about 100 yards and said that it was probably an leak in the innercooler pipe somewhere...my thing is if it was a leak would it still hold the boost at 6psi?? ...it is about a half pound lees than what it usually boosts at..all i know is it should have ran alot faster than 18 seconds in the quater,and it has never ran as bad as it is now!! any input is appreciated