yeah i know the key gets hot and i just ran the engine for 20 minutes and i got pressure in the radiator coolant in the top of the radiator coolant leaking out the bottom and i cleaned off the dipstick and put it back in, now i got milky oil so yeah i got a BHG fun fun fun but at least it...
im thinkin its a cracked hose because besides the coolant leak and overheating im not seeing any other signs of a BHG but anythings possible with a MKIII the temp gauge has only gone 1/2 way up never higher but i have coolant leaking out so im thinkin i got a busted hose and perhaps the...
hey guys i realize that stock is a truck type shifter and i am aware of the sogi mod but my question is the play in the shifter, when im in 1st gear 2nd gear 3rd etc it feels like im in neutral with the amount of wiggling i can do with the shifter
yes yes i am aware of that and i do appriciate ij taking time out to help me out i wouldnt upgrade anything relating to performance until my engine was 100% operational
im near the airport 436/lk underhill i gota do the compression test to see if the HG is blown if not im gona retorque it to 75lbs if i can find some help because i have no clue what im doing, and after that is done and my coolant leak is fixed speedo cable fixed, and running 100% ill add a DP TP...
oh im not driving it anyway until its 100% operational, i just dont have any cash atm really so i couldnt even buy the test lmao ill wait til i get my check if i retorqued it wouldnt i have to lift the head anyway? forgive the dumb question but i know nothing about this
how much is a lot exactly 1-2k? and no im not prepared ATM but if it isnt blown ill just fix the coolant problem and upgrade to a test pipe dp and exhaust til i have the cash to tighten the HG
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