So I ran a compression check today came out 200,190,200,195,192,200 I was pretty happy with this. Then I ran the leak down test. Cylinder 1, 150psi and holding. 2 holding, 3 holding, 4......shit! ::bhg::. 5 & 6 the same. Its a pretty slow leak through all 3 cylinders and I know the head was torqued to factory specs as it was a toyota crate motor, Ya big $$$ for the last owner. Im going to see if I can get away with retorquing the head until I park it for the winter. If not I guess its going in the garage early this year. The upside is I can get the intake and exaust manifolds along with the valve covers coated while they are off! Anybody recomend anything while I have the head off and apart? New valve springs maybe? I dont have plans for any outrageous HP #s