Having an intermittent misfire with my 1989 7mgte r154. Car was originally auto and manual swapped about a 2 months ago. The car is having a miss and stumble under load, and while it is doing this the car is leaning out. Its a stumble, to the point where the car jerks slightly. It is not hitting fuel cut, I know what that feels like. When it stumbles/misses, it is leaning out on my wideband.
So here's everything that I've done so far to the car:
all new couplers for intercooler hoses,
swapped coil packs w/ no change,
swapped afm's with no change,
new OEM plug wires,
brand new plugs gapped at 0.030 (no oil on plugs),
timed with ati crank dampner and rewired CPS,
brand new flow tested 550 injectors and lexus afm,
TRD air fuel pressure regulator (J-tube bypass),
OEM toyota fuel filter,
brand new and adjusted tps with new connector,
almost all new vacuum lines,
and new accordion hose,
rebuilt garrett turbo only pushing 4 lbs right now.
Car was misfiring before the new injectors, new afm, and fuel pressure regulator.
The last thing I could think of is fuel pump, or possibly fuel pump wiring as I have not done the 12v mod?
What's also weird is that one day I adjusted my clutch is the problem went away for maybe two days, then returned. Clutch is brand new, ACT 6 puck set up with maybe 2000-3000 miles.
Thank you for your time.
So here's everything that I've done so far to the car:
all new couplers for intercooler hoses,
swapped coil packs w/ no change,
swapped afm's with no change,
new OEM plug wires,
brand new plugs gapped at 0.030 (no oil on plugs),
timed with ati crank dampner and rewired CPS,
brand new flow tested 550 injectors and lexus afm,
TRD air fuel pressure regulator (J-tube bypass),
OEM toyota fuel filter,
brand new and adjusted tps with new connector,
almost all new vacuum lines,
and new accordion hose,
rebuilt garrett turbo only pushing 4 lbs right now.
Car was misfiring before the new injectors, new afm, and fuel pressure regulator.
The last thing I could think of is fuel pump, or possibly fuel pump wiring as I have not done the 12v mod?
What's also weird is that one day I adjusted my clutch is the problem went away for maybe two days, then returned. Clutch is brand new, ACT 6 puck set up with maybe 2000-3000 miles.
Thank you for your time.